The AEM10941 is a solar harvesting IC. It handles a small solar panel and charges either a lithium battery or a super capacitor. I ordered a evaluation board (part number: 3AAEM10941CPCX10) to test it out for the Cat Feeder Unreminder but I went ahead and made a footprint for it in Eagle. The evaluation board comes with a couple solar panels and some super capacitors to mess around with.
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Asbestos Testing
Decided to get the firewall insulation checked on the Checker for Asbestos… Just in case :)
Good news. None detected in the samples I set!
Parker’s Old Fashion Recipe
My take on the old fashion, developed after drinking many of them.
- 2oz Rye Whiskey
- Bulleit 95 Rye (Green Label)
- 1/4oz Simple Syrup
- Use a high quality syrup.
- I use Barsmith brand.
- Bitters
- Peychaud’s Aromatic Cocktail Bitter
- 2 Cherries
- Luxardo Maraschino Cherries
- No substitutes allowed.
- Orange for the peel
- Big Ice Cube or like 3 normal sized…
Grab a lowball glass and put your ice cube in there. Coat the ice with the bitters. Pour in the simple syrup and then the whiskey. Take a fork, and pull 2 cherries out of the jar. Drop them into the glass and use the syrup coated fork to “whisk/stir” the drink. Take an orange peel and twist it while holding it inside the glass. Drop the peel into the drink. Enjoy
Notes for experimenting. Depending on the whiskey or bourbon you will have to adjust the simple syrup ratio. Bourbon typically requires less as its smoother and sweeter.
Cat Feeder Unreminder: Concept
Ok, this is a project I talked about way back on Episode 237 of the MacroFab Engineering Podcast.
Its a small electronic device that makes sure you don’t overfeed your cat by feeding more often then needed. Low power consumption with no need of changing batteries or external power sources. Solar power? Basically a resettable egg timer that doesn’t need batteries cause if the batteries die then you won’t be reminded to feed the cat!
User interface should be simple. One button to reset the timer, then a LED that lights up when you are ok to feed the beasties and another LED that lets you know the system is working correctly. Maybe one led that is turned on when its not time to feed and then turns off when time to feed. Pressing the button resets and turns the LED back on? Verifying the circuit is still powered? Prevents hungry cats at least.
Simple BOM so far:
- AEM10941
- This is a Solar Energy Harvesting IC
- DSF505Q6R0JBG
- Super Caps
- 5F Capacitance!
- Solar Panel AM-1816CA
- 84µA at peak power
- This is specced at 200lx
- LTC2956
- Low power, configurable timer
Napkin math on power requirements. The LTC2956 draws 0.8μA. LED at 40uA. Total draw when Cat Feed Indicator is on is 40.8μA.
5F x (4.5V-3.6V) / 0.0000608 = 74,013 seconds -> 20 and a half hours!
So we have enough power from the fully charged Super Cap to run everything for almost a day. That is good. Should bump up the capacitance just to get a full day.
Github repo for the project.
Welded Dog Gate
This is a gate I built back in 2018 for my dog, King. Welded it out of 1″ square tubing and 3/4″ x 4″ cedar posts.
Updated the contact page
Old contact form was broken. Removed it and just put in some links to get a hold of me. Also disabled comments on the blog as its 99.999999% spam.
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where has time gone
Gas Tank Skid Plate Reconstruction
A common issue with Grand Wagoneers is rusting gas tank skids. Gas tanks on Wagoneers are plastic. To support the weight, the gas tanks are fastened to a metal skid. Then the skid is bolted to the frame. This is a great setup as the gas tank can not rust out and clog fuel filters but Jeep made the skid plates out of thin metal with poor rust prevention so they do not last.
I disconnected the fuel lines and fill lines then dropped the tank. Skid is full of dirt and rust. The straps that hold the tank to the skid where rusted through so removing the tank from the skid was easy.
I then inspected the frame where the gas tank lives. This is also a very common area for rust to happen. This looks bad but the frame was 100% intact. There was ton of dirt build up on the frame that at first looked like rust. The rusted holes in the left side of the picture is left over parts of the skid plate that was still attached to the frame. I cleaned up the frame and painted it with some chassis saver to prevent any further rust.
Then I cleaned up what was left of the skid plate. I was hoping to repair the skid by patching it but the skid was to far gone at this point.
Then pulled the skid plate triangle brace and cleaned it up. Swiss cheese steel. I decided to rebuild the triangle brace first since it will be easier.
Built the new bracket parts for the triangle brace. I added nutserts to make install easier later.
To make the rest of the triangle brace, I traced it onto some cardboard. Then I cut out the cardboard and mocked it up with the braces I cut out steel.
Then I copied the cardboard into some 14AWG steel. The steel was bought LTP (Less Then Prime) which means it is rusted but it was inexpensive. Cut the steel out and then cleaned up with a flappy disc on the grinder.
I then tacked the brackets onto the steel and compared it to the original bracket. Looks good to me!
Triangle brace is complete. Time to start fabricating the skid plate for the gas tank.
I started measuring the skid plate and started cutting some steel.
With the skid plate and triangle bracket fabricated and painted I installed the gas tank. Before that I cleaned out the gas tank with a pressure washer and dried it out. Then the gas tank received new gas tank straps, vents, vent hoses, and sending unit.
I then installed the skid under the wagon. Fit great and now I do not have to worry about the gas tank falling out.
Coolant System Repair on the Wagoneer
Time to start fixing things on the Wagoneer. It drives around town fine but when the engine is turned off after driving it tends to puke radiator fluid everywhere. Looking at the radiator it is clear this happens around the filler neck. Wiggling the filler neck it looks like there is a crack at the base. Since this is a brass/copper constructed radiator I should be able to braze/solder this back together.
While I am in here I am going to also replace the T-Stat, water pump, and clean up the heater box. Basically a cooling system rebuild.
Draining all the coolant. On the Wagoneer the drain peacock is at the bottom which is nice. On the TJ Jeep it is horizontal and tends to shoot coolant all over the steering suspension. Only thing in the way was the two transmission fluid lines which I was able to zip tie out of the way.
With the fluid drained I removed all the hoses in the system. There are three that attach to the radiator; Upper radiator hose, Lower radiator hose, and the hose that goes to the overflow bottle. I inspected these as I removed them and they looked to be a in shape and I will be reusing them.
I pulled the T-stat housing and it looks like it belongs on the Titanic. I will clean this up with a brass wire wheel on the drill before reinstalling.
The T-stat itself sits in a grove on the block and the gasket is put over it. The previous mechanic just gooped RTV all over it and was a pain to remove.
Not much left of the original gasket. Lots of rusty sludge build up on it as well. Makes sense that the Wagoneer sat for years before I got it.
At this point it makes sense to make more room to work by removing the fan clutch. Since the belts are still installed it makes it easy to remove the 4 bolts on that hold the fan clutch to the water pump.
Next I removed the belts. There is a nut on the bottom of the alternator that will need to be loosened. Doing so allows the alternator to swing inwards loosening the belt. A nut on the back of the power steering pump does the same thing.
I wrote down the part numbers in case I need more belts. The belts look fairly new so I am going to reuse them. With the belts removed I pulled off the water pump pulley to get a good look at the pump.
Oh boi, previous mechanic RTV the pump on with Black RTV. Gonna be fun to remove. There are lots of bolts on this thing and brackets that attach to other accessories. I removed all the bolts and laid them out in order of how they came out. The alternator bracket and power steering bracket need to be loosened so the pump can full come off. Removing the pump was not actually that bad as the RTV did not have a good seal on the surface.
Before I tried brazing the filler neck of the radiator I first removed the fan shroud as It is made of plastic and I did not want to melt it.
I cleaned up the filler neck area with a brass wire brush on the drill.
I coated the filler neck joint with lots of acid based flux and then heated it up with the propane torch till I could pop it off with some pliers.
After the filler neck came off I cleaned up the mating surfaces with the brass wire brush on the drill. Then I coated both surfaces with more flux and pressed the filler neck back into the radiator. Then heated up the joint again and brazed it with the solder.
Looks like I did a decent job. Will know at the end if it holds pressure :)
Since the T-stat housing area and water pump mounting surface was so corroded I hit the entire area with the brass wire brush on the drill. Cleaned them right up.
During the clean up I found that the previous owner just left this broken bolt for me to find. Woooooooo….
Looks like someone already tried to extract it as there is a hole drilled into it.
I finished the job by drilling a 1/8″ pilot hole into it and then used a #7 drill bit to clean up the hole. I then put in a 1/4-20 tap to chase the threads. If I ever sell this engine to someone I would go back and drill it out and helicoil it but this fix will probably work for what I need.
T-stat installed!T-stat installation was next. On my water related gaskets I like to use Permatex High Tack Gasket Sealant on both sides of the gasket. I know some say to never use a sealant or use only blue RTV but I have never had to go back and redo a gasket with this stuff. Unlike RTV the High Tack Gasket Sealant is easy to clean up if you need to replace the part again in the future. If also sticks to the housings better which is great when you do not have mounting/alignment dowels.
After the T-stat housing I installed the water pump and put the bolts back in the same way they came out. I looked up the torque numbers in the Factory Service Manual and torqued the T-stat housing and water pump to spec.
I then removed the studs from the old water pump using the stacked nut method. These studs need to be reused on the new pump.
Then I put the studs on the water pump. Then I put the water pump pulley on and reinstalled the belts but kept them loose till the end as I wanted to make sure I did not have to remove them later.
I then installed the fan clutch/fan assembly. To prevent the pulley from rotating as I was tightening them I used one hand to press down the belts which prevent it from rotating.
Installing the fan shroud was the last part of finishing up the front of the engine for this project.
Now I wanted to clean out the heater core box since I had the coolant out of the heater core.
First I started by removing the two external bolts and the blend door cable on the top of the heater box.
On the inside there are two more bolts that hold on the heater box. To get to these bolts the A/C module needs to be dropped from the dash. The A/C does not need to be discharged for this. There are around 6-8 bolts that hold it up under the dash. After removing the box kinda just falls down.
The easiest way I found to do this is to use lots of wobble extensions on a deep socket and snake this contraption in between the A/C module and the dash. Makes it fairly painless.
Then pull the heater box from the engine compartment. Mine had quite a bit of leaves that prevented the blend door from moving all the way.
The heater box opens up by removing all the bolts on the outside. There are five pieces; two external fiberglass shells, inner metal plate, blend door, and the heater core.
I took my heater box all apart and cleaned it up. Then I reassembled it.
First put the blend door back into the shell, next put the metal inner plate in. Next install the heater core and then the top of the shell. When putting the bolts back in do not tighten them up all the way till all the bolts and the heater core tabs at the top and bottom are all lined up.
With the box cleaned up I reinstalled the heater box and put the dash back together. Then reattached the blend door cable.I hooked all the hoses back up on the radiator and heater core and refilled the engine with new coolant and put a new radiator cap on.
A trip around the block and to the grocery store shows that the Wagoneer has stopped puking radiator fluid! Success so far!
New Vehicle Acquired. Jeep +1
This past Friday I picked up a 1990 Jeep Grand Wagoneer. It was in Dallas, Tx so I took the Friday off and drove up with my Dad and picked it up. Drove back to Houston with it (~300miles) was a pretty fun road trip!
It is a fully loaded Grand Wagoneer with all the trimmings. Everything functions except the rear window wiper and sprayer. The wiper looks to just be a bad wiring and the sprayer is missing from the back. If you know where to get a sprayer let me know….they seem to be unobtainium.
The 5.9L AMC 360 engine is mostly intact and runs ok. The valve seals are blown so the engine smokes a bit on start up.
When I got the Wagoneer the oil pressure gauge wasn’t working so I just had to hope it had oil pressure to make it back to Houston.
The first thing I did was an engine oil flush and replaced the oil pressure sender and wire. Engine idles at 40psi cold and ~10psi hot. The hot 10psi is not ideal but it does have 188K miles on it. I am debating rebuilding the oil pump or just leaving it.
My long term plan with the Wagoneer is to not 100% restore it but just make it nice. Fix all the problems, modernize the electronics, and swap in a LQ4 V8 engine and 4/5 speed automatic transmission. To get there however will take time.
My short term goal is to turn it into a decent daily driver and rock the AMC 360 engine while I fix the major problems and figure out how much I want to restore.
Here is the “short term” list.
- Cooling System
- Radiator has a cracked filler neck. Fix the copper/brass radiator by soldering/brazing the crack
- Replace T-stat
- Replace Water Pump
- Flush System
- Replace temperature sender
- Engine
- Another engine oil flush
- Open valve covers to check rockers and push rods
- New spark plugs
- Transmission
- Oil flush
- New filter
- New fluid
- Fuel System
- Repair gas tank skid
- Clean tank
- Replace rubber hoses and steel if needed
- New fuel sending unit
- Tank vent and hoses replacement
- New fuel filter
- A/C (very important!)
- Recharge R12
- Fix electrical
- Steering
- Replace leaking steering gear box
- New hydraulic hoses
- New fluid for power steering
- Ball joints
- Tie rod ends
- Suspension
- Replace sagging leaf springs with new suspension
- Drivetrain
- Flush and replace oil in transfer case
- U-Joints
- Rebuild Axles
Sounds like a lot but afterwards it should be a nice daily. The Wagoneer already rides like your sofa going 70mph down the freeway so it can only get better!